Well guys update on AnaSTasia.
After pull carbs again double check everything, check coolant leak all good.
So I lube up the manifold boots and the carbs seem to go back a little easier this time, maybe just practice.
Check all linkages vacuum lines, hold my breath Ignition blast off, still needed choke once again no idle,
So adjust idle cable and manage to maintain idle at around 1100-1200rpm.
Pull out Yorkies carby sync tool
Check No 4 which is base reading 5.5
No 1 10.5
No 3 8.5
No 2 7.5
A little bit out one would say, so I adjust all and reduce idle to normal and guess what I have idle.
However still note quite right, so for whater ever reason I stert pulling of plug leads.
Remove No 2 lead very noticeable change.
Remove No 4 lead same result
Remove No 3 lead same result
Remove No 1 and almost no change and as I pulling cap out of plug hole i notice the end of the cap arch all the way out.
So I think its fair to say lead may be faulty, all the others no arcing.
Maybe fair to say my problem all along, why didn't I check 1st don't know.
Anyway my Carbs are nice and clean .
So Yorkie please add to my list of goodies I need to pick up from you.
Cheers